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We celebrated our 42th anniversary on
March 27, 2007.

Donna & I have a 1928 Model A Ford Open Cab Roadster (convertible) Pickup
Truck.
It is a Type 76A with a Type 78A bed. The serial number is A120955A
and was produced
in May of 1928. It is 1 of 24,000 produced in 1928. I
believe that only about 100 of
these "Open Cab's" are still in existence. That includes
all 4 years, 1928 thru 1931.
It has a top speed of 65 mph.
I've only had it up to 55 mph - that's enough - no sense in taking any chances.
I don't want it to put it under any undo stress.
Tare weight is 2073#. Wheelbase is 103.5".
Compression ratio is 4.22:1.
3.875" bore X 4.25" stroke = 200.5 cubic inches and develops
40 brake horsepower @ 2200 rpm.
Original list price was $445.00.
I purchased this truck in June of 1998 from a man in
An interesting note: as Secretary of the
local Meat Cutters
Although not 100% authentic, my pickup
is close enough to fool all but the purist. I consider it "customized"
and nothing has been changed that can't be returned to
authentic. For instance, the original truck did NOT have a
top that folded down - mine does. The original top could be
removed - but not folded. The original truck was painted "Rock
Moss Green" lacquer body with black enamel fenders. My truck is
2002 Ford black basecoat/clear coat. The original truck did NOT
have a chrome radiator shell or horn. They were both black. Wheels
on the original truck were 21" and painted black. I have the 30 - 31
Model A 19" wheels and they are powder coated and clear coated
to match the interior and top color. The original top was,
also, black. The original truck had no outside door handles. The
'29 door handles have been added to mine. My truck has rear bumpers - not
so on the original. So, you see - my truck, though not 100%
original - is just "customized".
I've entered several shows resulting in
three 1st, a 2nd, a 3rd and the oldest car trophies. My proudest
trophy is the
Because of a minor traffic accident on
Attending Car Shows with a
driver tends to be a real chore. It is necessary to continually
load up spare parts (in case of break down), tools and detailing
supplies. When you get to the show location, everything must be
unloaded and after the show load it all up again and, again, unload it all
when you get home. Well, seeing some of the street rodders and motorcycle
guys having a small utility trailer to carry all of that stuff, I got to
thinking how convenient it would be to have one.
That was the simple part -
thinking of what to do. Where to find a small trailer light enough for
the Model A to pull - yet big enough to handle the necessities - that was the
real problem.
I looked and looked.
The closest thing I found was a car top carrier with wheels offered by J.C.
Whitney for $600. It just did not look sturdy nor large
enough. I checked out some of the street rodders. The really nice
ones were a cut down version of their car. I looked at a few
trailers made from modern pickup beds. They were too heavy. But,
that got me thinking. Why not a trailer made from a Model A Pickup
bed? Well, again, that was the easy part. Have you looked for a
Model A pickup bed lately? Hen’s teeth would be an easier find.
Since the local Model A Club (50th
Anniversary Chapter) offered free want ads in the newsletter I decided I'd
give it a try. Several months passed after my ad was
published. Finally a Club member from
Time passed for another month
or so. Then one evening I got a call from another fellow about 50
miles from me. He said that he had a frame that at one time had a Model A
pickup bed mounted on it. He said it was complete with rusty wheels
& bad tires. To keep it light, the builder had used 1"
square tubing and a Model A front axle and welded the spindles to run
straight. That was a real novel idea - and it works. Again, I
told the seller that the frame was mine and would retrieve it soon.
I started recruiting friends
with pickups that were willing to assist my voyage to retrieve
the purchases. Within a couple of weeks I had everything back at
home with the assistance of my friend Earl Cloud.
Wouldn't you know it - they
belonged together. The original builder, Doug Zhan, told me that it
was fabricated in 1985 and pulled 25 miles one time behind a Bronco
just to get it home. The original owner made the weather proof top, covered
it with Model A Sedan Vinyl material and used a Model A door handle as a
latch. The color was a dark brown that matched the Coupe of Club
member, George Millar, the original owner. I needed it to be
black to match my pickup. I found a local painter that picked up all the
pieces, put them together and painted it 2002 Ford Explorer Black
basecoat/clear coat. We powder coated the wheels to match the
pickup and installed new, matching Firestone tires. I had a local
welder custom fabricate a draw bar on the pickup so I could use a standard
2" bar & ball and interchange with my Explorer.
Now, you ain't never seen
anything better. This thing is great and does exactly what I
wanted. The center of gravity is forward and has 0 tongue weight so I use
a 6" drop down hitch. It does get a little loose above 50 m.p.h. -
but I don't drive the Model A any faster than that anyway. I would
really hate to see more of these since I like to have things no one else has,
but if you have similar needs - this is it!!
As if my pickup
alone didn't draw a crowd, now with the trailer it's awesome!!
BACKGROUND INFO
My 1928 Model A Open
Cab, Roadster, Pickup, Type 76A is a daily driver. The
motor gradually developed a knocking sound with volume increasing
with mileage. After several attempts at adjusting the shims, the mains
were checked and found to have the babbitts literally "falling
out" in chunks. The motor had been rebuilt by the previous
owner about 15 years ago but had very low miles since. The lead was
obviously of poor quality. It was determined that new babbitts MUST be
poured. Since the motor had to be pulled, it was decided to do a complete
restoration.
In October, 2002, the Pickup
was completely disassembled.
The motor was found to be in
excellent shape, except for the babbitts. The cylinders had been
sleeved to .000 and the crank was at -.010. The valves needed only a
slight grind to seat perfectly. New rings were installed and new babbitts
poured. Each mechanical part, including nuts, bolts &
washers, was either repaired or replaced and all the body
parts were repaired of all defects and individually primed with black
epoxy primer and painted 2002 Ford Explorer Black basecoat/clear
coat. The fenders had rubberized undercoating sprayed onto the underside
to absorb rock impacts. The bright metal was either polished or
replaced. Imported from
New rear motor mounts and a
front "Float-a-motor" were installed. The 6 volt starter,
generator, distributor, plugs and coil used were the same ones
removed before rebuilding the motor, which was running excellent except for
loose babbitts. New plug wires, distributor upper plate, lower
plate, body, shaft, condenser & points were installed. The oil
pump was rebuilt. The water pump was rebuilt with leak less nut
& stainless steel shaft. The radiator was boiled out.
Rebuilt Houdalle shocks & links were installed. New seals were
installed on the rear axles and 1 brake lining was replaced due to grease
leakage. New brake rods, cross shaft, clevis pins and stop light
switch were installed. Modern, threaded grease zerks were
installed. The intake and exhaust manifolds are the same
ones removed from the motor before it was rebuilt and were NOT surfaced
but were checked with a straight edge. A new "one
piece" gasket was installed. The throw out bearing &
clutch assembly were not worn and only the linkage was tightened up. A
new wiring harness, battery cut-off switch, ammeter and ignition switch was
installed. The steering was all new and no adjustment or replacement was
necessary.
THE
PROBLEM..................
Well, after its total
restoration, the pickup was ready for a test drive on
Ready for the final test
drive, when attempting to start it - a gun shot
backfire occurred. Then, pressing the starter button again, it
started just fine. Everything was great on the test drive for about
30 minutes until stopping to get 5 gallons of gas.
When restarted, it sounded like it was running on 2 cylinders and had
a clanking noise (like a loose valve or lifter). It had barely enough
power to pull away from the pump to get out of the way. The distributor cap
was pulled; the points, rotor, body, etc. were checked. Seeing
nothing strange, it was re-assembled. Starting again, it was
better than before - but still not right. A one mile
trip back to the shop was made with a top speed of about 25 mph
(and several unhappy motorists). The original timing and point settings
were perfect, however, after getting back to the shop - it appeared
that the timing had changed and was very far off. Again, after resetting
the timing and points, it ran good again.
This was the first
diagnosis: (by Bill Barlow)
What has happened is a
valve, probably an intake, has stuck open. This will cause the gas to explode
back through the carburetor causing the backfire you heard when starting. The
valve then freed up until the engine was warm and caused the valve to stick
again. This would account for running at least one cylinder short. It would
probably still start but with an open valve that particular cylinder would not
produce any power.
Take out the spark plugs
so you can look in onto the top of the valves and see if you have more than two
open at the same time. If so tap with a wooden dowel until you find the one
that is stuck in the open position. You may have to disassemble the engine to
get it working freely.
One other thing, it could be is a blown head gasket if you didn't
re-torque the head nuts after the first warm up.
FIRST MAINTENANCE
PROCEDURE
The plugs were
removed and visual analysis could not see a valve staying
up. "Marvel Mystery Oil" was squirted on each
stem. Another 5 gallons of gas and 1/2 qt of Marvel Mystery Oil were
poured into the gas tank for additional lubrication. The car drove
about 15 miles with no problem. In fact, it really ran excellent up to
about 45 mph for short increments.
/smaller>/fontfamily>The next day
it idled about an hour - no problem.
/smaller>/fontfamily>The next
day, the original problem reoccurred - running on (sounds like) 2
cylinders. It ran only about 2 minutes.
/smaller>/fontfamily>The next
day, again the same thing - 2 cylinders. Again, running only
about 2 minutes.
/smaller>/fontfamily>The next day -
same thing. All the plugs were removed and, again, each valve
could be seen moving up and down. The plugs had some carbon -
not lots - but some. The distributor housing and rotor (new
parts) were cleaned. The plug wires (new) look
good. The timing has been checked and reset many times and it
has always looked good. Some blow by could be seen around the
muffler clamp but none anywhere else.
/smaller>/fontfamily>3
different rebuilt carburetors were installed with no improvement.
SECOND DIAGNOSIS: (by Bill Barlow)
I know the distributor
body is new but it may have a defect causing two cylinders to short out. If you
have another body I would give it a try. I think we already tried the grounding
of the plugs while the engine is running to find which plug or plugs are not
firing. If all four plugs are firing when they are supposed to and it is still
running on two, it has to be in the valve train.
SECOND PROCEDURE
Compression checked 60# on
each cylinder. Therefore, no leaks and no sticking valve.
Each plug was getting at
least 1/8" spark jump.
The plugs were
shorted one at a time and found that #1, #3 & #4 made no
difference in performance while shorting #2 killed the motor.
It was running on 1 cylinder! No wonder there was no
power.
Again, 3 different
carburetors were installed with no difference.
So, just to be certain that
everything was eliminated one part at a time, "TDC" was
found using the timing gear indention; another new set of points
& condenser were installed as was the spring under the upper plate; the
coil voltage was checked as was the coil wire. The
new brass plug wires were cleaned. Timing was set using the
procedure shown in the "Technical Questions" section of the M.A.F.C.A.
web site http://www.mafca.com.
Still no difference.
THIRD DIAGNOSIS: (by Doug Zahn)
The local "Technical
Expert" and my Model A engine rebuilder was contacted for
advice. He said it sounded like it was trying to run on air. He
thought it may be a leaking manifold gasket or cracked intake manifold and
suggested replacement of the manifold gasket.
THIRD PROCEDURE
So, the manifold gasket
was replaced. Trying to make it easy and save time, the manifolds were not completely
REMOVED , just loosened up enough to get the old gasket out and install a
new one (without sealant). Well, that was a lot of wasted
time and ruined the new gasket. The motor was still running on 1
cylinder. However, that did tell what was wrong - the manifold gaskets
were leaking. So this time, it was done correctly by
completely removing the manifolds. The new gasket was starting to
be burned after only 2 minutes of run time. This time the manifold was
checked completely for cracks, flatness & straightness at a machine
shop. Both manifolds were both ok. The manifolds were
cleaned of all old burned gasket material & sealant and polished with
some 400 emery. The block surface was cleaned really
good. "Red", high temp, gasket sealant was applied to the
manifolds assuring that it would provide a complete, nice and smooth
seal. The new gasket was installed onto the manifolds. After
letting it set up for a few minutes, sealant was applied to the engine
side of the gasket and allowed to set up for a few minutes.
Fearing that the manifold
nuts were bottoming out before actually tightening up the manifolds
against the gasket and giving a false torque reading, flat washers were
added between the nut and the cast iron washer. Since the cast
washers are NOT FLAT, care must be taken to make certain that they are
installed properly - the high side goes toward the nut. The nuts must be
torqued from the inside out at 55 lbs. and rechecked after getting hot and
cooled off.
The final solution??????
Well, guess what - still no
change. The motor was still running on 1 cylinder.
FINAL DIAGNOSIS: (by Doug Zahn)
Being told that if that
doing everything above did not fix it, replace the
plugs. And if that did not get it running ...................
FINAL PROCEDURE
All the plugs were
pulled and only #2 showed any sign of firing. The other 3 were only
wet. Wet???? That means they are now getting gas and just
not firing. Well, it just so happened that a set of new plugs
were in the tool box and in they went.
It fired up so fast I
almost wet my pants!!! What a sound. Nothing else sounds
like a Model A. Success at last. A
75 mile cruise was taken the next day,
Evidently the manifold nuts
did not pull the manifolds tight causing the gaskets to leak and fouled
the plugs. These photos show the gasket
that was blown after running less than an hour.

You just have to take your
time and eliminate one part at a time. The Model A motor is so
simple that everything MUST be right.
I want to thank each and
every person that offered advice, personal experiences and sympathy during
this exercise and especially Robert Wade that did almost all the mechanical
work, Martin Brown in assisting Robert, Jon Haydon for his technical
advice, Doug Zahn that did an excellent rebuild of the motor and offered his
superb technical advice, and Bill Barlow, MAFCA Technical Director. The paint was done by Tim Goyne, Goyne’s Body
Shop in
I won
I hope you enjoy my story and photos.

___________________________________________________________________________________________________________
I bought a 1928 Tudor
This car is all original. NO
Dents, only one small rust spot AND IT RUNS!!!! I drove it onto
the trailer to bring it to
This photo will give you an idea of what it looks like now.

That's the "Original" 1928
I am active in the 50th Anniversary Model
A Club, the
Donna bowling.
She has 26 700 series & 2 300
games. Only 2 other females in
She is always busy attending tournaments in
With a team score of 3,208, Donna’s team, “G.
G. Girls”, won 3rd place in the 2003 55th Annual Arkansas
Women’s State Tournament held in Jonesboro.
Her team mates were Cindy Covert, Debbie Ueckman, Felicia Burlison &
Peggy Cromwell. Donna finished 5th
in “All Events Scratch” with 1,761. Team
mate Felicia finished 1st in “All Events Scratch” with an 1,865
score.
Most of Donna's family is in
Donna enjoys riding in the Model A's, however, will not drive one. Maybe when the Tudor is finished I can get her to drive the Tudor while I drive the Pickup. What a caravan!!!!

Our oldest son, Gary lives in

Gary & Londa and their bikes.

Grant, our youngest son, a cook, is an E6, Staff Sergeant in
the HHC Company of the 82nd Airborne in
Previously he was in the 1st Battalion, 30th Regiment, 3rd Brigade, 3rd
Infantry Division, Mechanized stationed at
Grant has 2 daughters, Jacquline is 13 & Katelynn is 11.

The newest addition to Grant’s family is Garrett Lantz.
He was born
We really miss seeing them.

We smoke brisket, ribs, turkey & pork butt. You can't get better
"Q" anywhere in the world.
We always have some good eats!

I have an Oklahoma Joe "Chuck wagon"
smoker. I use only "

Here's Katelynn knawing on a rib bone.
We live in
We sell through Dealers, worldwide,
and on
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using the nickname "typewriter-man".
Click here to go to the GEORGE BEYERS COMPANY web page.
George & Donna Beyers
Telephone 501.776.1399
1500 Sharon
Road
Fax 501.776.3986
Benton, AR (Arkansas) 72019-6122
Cellular 501.776.5155 or 501.840.2000
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email me at gbeyers@ipa.net
or gb@georgebeyers.com
or Donna at dgbeyers@sbcglobal.net or db@georgebeyers.com

Come back and visit, often.
I'll have more photos posted later.
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